Tuesday, 1 December 2009

Underseal, underseal and more underseal

I have been slightly unmotivated by the task of removing underseal from the bonnet. I did however manage to spend a few hours last night by this tiresome task. Only good thing about it was that it kept me warm!

I am almost done with it - I guess it will be ready for the sandblasterafter next session.

The bonnet was worse than I had hoped. The left hand wing will have to be replaced. And some repars around the headlamppanel is also needed.
Bit of pics.






Monday, 12 October 2009

bit of this and that

Ages since my last update. It is not exactly as if I have been doing nothing. On the spitfire I have done next to nothing - not even bothered to adjust the dampers. And foolishly I have managed to misplace both set of keys for the car, so it is sitting miserably in the carport these days. Actually the keys werent misplaced - I had a moment of paranoia and hid the keys very weel for the instance the house would be burgled while I was away. When I needed the keys 4 days later I couldn't remember where I had hid them :B They will turn up eventually - hopefully before spring!

So basicly what has been done to the spit this season has been putting almost 3.000 miles on it and done nothiong but an oilchange and new oilfilter (well, then the insurance has sorted out new bumper and fixing the bonnet, but that does not count!)

On the GT6 major work is going on. Most of the car has been taken to bits now.







I am currently removing old underseal (waxoil?) from the bonnet, so it can be sent of to the sandblaster. The bonnet is far worse than expected. I will most likely have to replace a wing plus the panel under the headlight. :-/

Fair bit of filler around the headlight panel :o








:'( :'( :'(



Removing underseal is a pain in the whatever - especially when the car has been left for 20 odd years in the california desert. One should thing it was dried out and easy to remove - but no - it has more or lees been burned into the paint. Actually I am removing more paint than undersealer.







Do notice that the yank who was the previous owner of this vehicle did not believe in welding - he has obviously put all his effort into soldering the car together!!!!

Wont be pretty when it comes back from sandblasting!

Thursday, 3 September 2009




Friday, 7 August 2009

Taking GT6 apart

After a long vacation, it is time to get on with the GT6. The spit is with the painter. Need a respray of the bonnet after the reversing woman incident...

Anyway - was in the garage yesterday. Has been pulling all interior and doors from the GT6. It turned out that the tank was completely shot. A good example has been sourced.
Last night was "pull the dashboard" night. Was a bloody nightmare. Basicly the dashboard are held in place by the gauges. Unfortunately the small knurled knobs were rusted solid to the studs on the instruments. And it is so cramped behind the dash that I could not get to it with any tools. Amazing where this car is rusted - the sills and floors are spotless - but the gauges - oh horror!



I spent the better part of 2 hours removing the dash! The dash itself has pretty much disintegrated - will be a right challenge to get it sorted. Great fun ahead!

I suspect the former owner of this car was either a plummer or just has a serious fetisch for bathroom accesories. The draintap on the batterybox was this



and even worse - a bog roll was used on the steeringcolumn for unknown purposes (unless the car was used as a loo!!)

In an attempt to reduce heat/noise the former owner also glued foam all over the car (as seen above). Had a party removing all this. Nasty stuff. A really bad idea fitting this kind of foam - it absorbs moisture and had it not been removed car would have suffered in the danish climate.

Bits and pieces.

Bulkhead is soon cleared - master cylinders and pedals has been removed. Starter solenoid and wipermotor are also gone. Batterybox was some homebrew thingy riveted on - was a bliss to se it gone!
Next time the heatermatrix will be out, and I can proceed on removing the engine. On seciond thought - might leave the engine in until I am done with the chassis. Rear valnce is doomed - will soonish be replaced. Progress really depends on when I will get the spit back from the painter - I will need to prep it for Round Denmark Reliability Run which is in 6 weeks. Uh oh - I am in a busy...

Tuesday, 16 June 2009

CRASH, crap ........

Crap. Women should NOT be allowed to drive >:(

I was in town witing for the lighths when some woman decided to reverse her car into mine. She didn't see me - she said. :'( :'(

Bumper is dead. There is a kink in the frame just behind the rad - I fear the left hand side of the frame has been lifted.

Paint has cracked on the bonnet where the lamp panel is joined with the centerpanel.

Shit






Monday, 8 June 2009

Stats of the day - Gavnoe

OK - was at the autojumble on Gavnoe. Wether was arite - not fantastic - but at least not raining! I got up at around 6 oclock in the morning. Grapped som coffee and headed south. Got lost around Roskilde and switched on the satnav. Said I would be 17 minutes late for the meetingpoint. Booted the car - turned up 7 minutes late. Entered parking lot sideways :-)
It was bloody cold - next time I will be wearing gloves!
Back home (add another 50 kilometers that wasn't logged before I turned the satnav on.)


Car is running close to fine, but still need alot of adjustment. Dizzy is crap and cant wait to get rid of it. Shaft is slightly bent and car is running very uneven with a lot og missing beats. Bring on the megajolt please! Need to get the wiring sorted!
We had a good run from the meeting point to Gavnoe. Got to check out the brakes a few times. I love those mintex pads. Locking the wheels is no problems - especially when the pads are warm.
My spit next to Peters very nice TR4
Dirks Spit Mk2/Mk3 hybrid.


Lovely GT6 engine department




More spits

Nice steering wheel! (but probablu pretty uncomfortable on the long trips)

Well sorted TR4

With proper tyres!

Saturday, 6 June 2009

Prepraring for Gavnoe

Got a bit of driving last few days. Went to see hillclimb yesterday. Good fun, and the lonely Triumph did very well coming in second overall.

Tomorrow is Gavnoe Autojumble, which hopefully will be graced by nice weather. I went to a mate today and who was so kind to get the carbs in perfect tune. Found out the dizzy has a slightly bent shaft causing all a somewhat uneven engine. I reaaaally look forward to megajolting it!!!


Come autojumble tomorrow and hopefully some nice pics. Here is a pic of my car last time I went - think it was 2001. My spit mk 3 with the missing front valance. The short big bloke resting his hand on the window is the previous owner. All the panels you see in the pic has been replaced since the. Front, door, sills, windowframe, rearwing, bootlid. It didn't look to bad from a distance but it was very very bad! Actually - the only thing in the pic still on the car is the wiperams and the front bumper......

Tuesday, 26 May 2009

It drives

Isn't it great. There is absolutely NOTHING to report. Car drives - gives me a good 20 minutes therapy each morning commuting to work, and then again in the afternoon. Nice ride through the forrest. Excellent. I need to adjust the carbs and ignition. Can't really be arsed with ignition - I will megajolt it sometine in the future. So it's max a question of using to minutes on the ignition.

Carbs are completely out of balance and running to rich. I broke the choke-cable holder thingy - so cars is running with a slight choke permanently. Need to adress that one!

Thursday, 21 May 2009

Back on the road - life is wonderfull

Been a while since last update - been busy with all kinds of non-triumph stuff. However - there has been progress - car is now back together, brought home and put into daily service. Nice feeling. My clutch release pin operation has been a succes, biting point is now exactly where I want it - right in the middle of the pedal travel. This small mod making the pin adjustable is really a wonderfull thing.

Here is as pic of the modded pin and an old one for comparison


Love the feeling when things work out as planned.

Braking was a new positive experience. I had gone from noname cheapo pads to Mintex 1144. Brakes like a moderne now!!! Again - wonderful.

I took the exhaust of a while bace in order to refit gearbox. I took the opportunity to correct a minor flaw. The exhaust had been blowing - just a very very little bit due to the joint from 2 to 1 not being equal lengths. I chopped a ring of the exhaust. Another problem of the list. Wonderfull.




As a positive sideeffect - the vibration I had round 55 mph has gone as I rotated the propshaft - Wooooonderful.

So all in all - everything is fine. After a good long drive last night I checked the plugs. I really need to get the lambda sensor fitted so I can get some more info on the AFR. Plugs looked like this after 30 miles cosy driving.

Plug 1: (closest to the radiator)


Plug 2


Plug 4


Maybe a slight on the lean side??


Project now is getting the interior trimmed decently. And fix the sidewindows. The are deadstuck in the middle - and for the worse. I suspect some quick and dirty assembly of the doors are to blame. Seems that the winder mech is interfering with the doorskin - making an outward going dent - not so wonderfull.....

Thursday, 7 May 2009

Tapping for Megajolt

First - sorry - no pics. When I wanted to get a few pictures I realized (again) that the battery on the camera was flat. That's second time recently this has happened. Better get some fresh batteries soon.

Still - I have had some fair progress. The exhaust prop and engine are all bolted back together fine. I took the inlet manifold of and drilled 4 holes in it for vacuum. First a 2mm pilot hole. Then a 4,2 mm hole and finally tapping for 5mm thread. Went quite smooth was OK result. I have had some problems with the choke sticking. It is a SU1.5. It has been converted from waxstat jets to proper jets. Problem is (I think) that the links used to convert isn't all perfect and creates a bit of tension. Morten and I tried messing with the links to see if we could release a bit of he tension. After quite a bit of fiddling the choke got better - not perfect - but better. Carbs went back on - all nuts on the manifold studs were tightened.

I found out I had forgot to put the radiator overflow bottle back on when I put the radiator in. Bit of a problem as the radiator has to be tilted a bit to get to the bolt where the overflowbottle-bracket attaches. So - undo 6 radiator bolts - overfowbracket in. Tighten bolts again. Mission accomplished.

Finally I put in a very neat bit of wire harness that The Mad Welder had made for me. I am converting from dynamo to generator plus a few other thing. So I needed a new harness for the generator, the oilpan temperature and halogenlights. But it was made perfect and very easy to fit. Thanks Morten

Enough for this time. Next time I get to spend a bit of time with the car I will try and start it.

Saturday, 2 May 2009

A few steps forward again

After a few setbacks thng are progressing again

Gearbox has been bolted back on the engine. I har to take prop ang exhaust off to get to the gearbox - and now the exhaust wqs off I used the opportunity to get a few things right. The joint from 2 to 1 was never really good as one pipe waqs a bit longer than the other. I pulled the manifold and made a cut. Now lengths are perfect. I also made another bracket to hang the exhaust by on the differential. It was onky attached on one side making the two exits not sitting even.

Exhaust and prop are now back on - and theoretically I should be out enjoying the fine weather. Ahem - now everything waqs off I couldn't resist taking inlet manifold off in order to tap holes for the megajolt vaacum takeoffs. It needs four holes tapped.

I was going in circles round this job last night doing all kinds of other stuff. Perhaps I get a chance later this weekend. I don't really like the thought of messing up having the takeoffs looking weird pointing in all directions. I have t get the drill and tap entering manifold at exactly same angle. Better not rush this job.

Also need to work a bit on the choke. It is sticking. A bit of fettling with grid 1000 on the jet should help - hopefully....

Thats it for now

Monday, 27 April 2009

Triggerwheel attached to front pulley

So - despite my cars effort to piss me off there has been some progress. Triggerwheel has been attached to the front pulley.

First - clean pulley - find out how to position triggerwheel - done a while ago


Next - engage The Mad Welder to do his thing


Finally - put nut back on and tighten it well. Rad in.

Things are brightening up

Friday, 24 April 2009

One step forward - and 10 backwards :-(

The plan:
  1. Put exhaust on
  2. Put front pulley on
  3. Put radiator on
  4. drive and enjoy the 20+ celsius weather this weekend

Reality:
  1. Put exhaust on
  2. By accicdent drop a nut down into the exhaust - I fear the unlikely event that it will be drawn into engine by bacjpressure
  3. Take exhaust of
  4. Remove nut
  5. Refit exhaust
  6. Put frontpulley on
  7. Try to tighten nut to 150 lb/ft, engine turn, hhmm now what
  8. Put car in gear and slam the brakes
  9. Find out that something is very wrong with the clutch
  10. Diagnose shows that idiot me has NOT managed to get the clutch actuator pin into the slavecylinder
  11. Cry for 10 minutes
  12. Undo all bolts round bellhousing
  13. pull gearbox back - realise that this does not offer enough room to get pin out
  14. Exhaust and prop must come of
  15. call it the night - i give up
Off course batteries on camera are flat. well just enough power to get lens ut - but not in again

Lets realise - I will not enjoy a drive next sunday - it will be well into may before I get all this sorted.

Friday, 3 April 2009

Pick-up sensor and triggerwheel for MegaJolt

Last night in the workshop had one purpose - find out how to attach the triggerwheel sensor. When sensor is placed I will know where on the pulley the triggerwheel has to be, as the sensor has to point 9 tooth before the missing tooth when engineis at TDC

First I knocked up a very rough template for at bracket (no points for aesthetics!) which can be seen here






The triggerwheel had been attached with clamps, so could easily be adjusted so the sensor would point at ninth tooth.

With this position, TDC would be appr. at third tooth



Now - mark it - and leave it for the mad welder to attach to pulley while I am taking a well earned vacation under the sun waaaaay down south :-)



The bracket will be fabricated when I get home again. Initial thought had been along the lines of some angled iron. I have deserted this thought when I saw the rough mock up. I might just make the bracket from heavy gauge iron without angles on it.

This gauge should just about do it.



Friday, 27 March 2009

BUSTING BRAKES

In an attempt to improve braking I have fitted Mintex brakepads to the fronmt of the Spit. To avoid glazing of the pads I decided to bust the surface of the disc.

So caliber of, and start rubbing with rough sandpaper. The disc have a slight blueish/brownish tint which dissapperar after a little rubbing with grit150 sandpaper.






Ideally disc should be machined, but time is short, havent got the hardware for it and really didn't want to disturb the bearings.
After a while (10 minutes each side of disc) disc had got the right slightly rough surface, and all the miscoloration had gone - clear silver!
Next find pads - mintex at the left, Countys finest at the right (500 miles wear on them)



I fitted the anti squeel shims, and slammed the entire bit together.



Job done.



Daniel R. (aka SpitmkIIICPH) came by and dropped off a much needed lift. It is more rusty than rysty, but will hopefyllu clean up nice and work. A lift is defo needed. I can't get under the car anymore. I say it's because car has been lowered - some says it's because I am getting old and fat!

Anyway - here is the solution. Just needs a lot of care and grease/paint/slight repair








Sunday, 22 March 2009

Round Denmark Reliability Run

Do not forget this years Round Denmark Reliability Run.

http://rdrr2009.blogspot.com/

Anyone interested can mail me direct at nikolaj.blomberg@gmail.com for more info

It's the weekend 18-20 september.

1250 miles in 36 hours.

Cheers

Saturday, 14 March 2009

Fooling around with ignition coils

A few mates and members of the Danish Triumph shared my interest in finding out - what is unside an ignition coil, and is there any significant difference in power output of traditional oilfilled coils vs modern dry coils

We made a simple test bench from an old distributor and a battery. Looked like this




Next step was to test the coils: an unipart coil, a lucas sports coild and a modern dry coil

The very scientific test was to experiment with how long a spark the coil could draw, and look at color and "fatness" of the spark.

In action it looked like this



There was no doubt that the modern coil supplied the longest and warmest spark. In second came the lucas sportscoil, but only marginally better than the Unipart coil. I doubt there would be any difference in car - at least not any that would justify the extra cost!

Now to the fun part - take the coils apart (boys will be boys...)













There was no big difference between the coils. The lucas coil had more windings, but basicly same construction.

Great way to spend an afternoon with good friends :-)

Thursday, 12 March 2009

Going down with 0.00000197285353535 MPH

Or in other words - I managed to install a rear lowering block on the spit. What I thought would be really simple (still that naive yes!) turned out te be a 4 hours task. The rear suspension being a swing spring does not make matter easier....

I loosened the spring - lifted it a bit and tried to place the lowering block on top of the diff. Then putting the spring back on. Fiddle with diff studs (long type). Hmmm, something was defo wrong... Toiook me about one hour to figure this out. Thought I just had the studs misaligned.

First I found out that either the spring were to wide, or the recess in the lowering block were to narrow. Either way - they didn't match :-( Fettled a bit with a file, and in some 15 minutes it was (theoretically) suitable to go on the spring.

Back to the car - try to put the #¤%#/ bock on again. Turns out that either the stud on the spring isn't properly centered - or the hole in the lowering block is to small.

Block out - find the file - enlarge hole. Another 15 minutes gone. Swear a bit. Drink a cup of coffee.

Back to car- hooray. Block fits on spring. At this time I was easily distracted, so when a mate came by I took a break.

One hour later - back to block. Now the challenge were to get the studs past the block and down into the diff housing.Not easy as the block is shorter ythan the diff, so there is really nothing to go by.

Eventually I had the spring/block and diff holes lined up. Studs went in fairly easy. Then washer and a nylock. Voila - car is now half inch lower - in just 4 hours - which makes car going down at the terrifick speed of 0,00000197285353535 MPH. ;-)

Friday, 6 March 2009

Progress

Surprisingly amount of progress last night.

Task one: fit shorter springs and adjustable shocks to drivers side - only managed passengerside last week before I ran out of time. Was easy. No complications. Undo lower shocker bolt and lower trunnion. Remove old shocker and spring. Relase spring. Steal top hat. Fit the new spring and shocker. Admire ;D

Impressed by myself I started to removed radiator for the next task: Undo pulleynyt in order to rectrieve pulley so I can put the triggerwheel on it. Radiator itself was pretty easy to bolt of. But the hoses was as glued on. After a fair amount of swearing it all came of :)
Next, the pulleynut itself. Tried turning it - no luck. Stuck on tight. Well done when engine was assembled last year.... Next move - let the starterengine free it. Worked like a charm ;D A few good wack with the starter and it spun of.

As I was obvoiusly on a lucky streak I went to the rear of the car with a lowering block in mind. I had forgot the block itself at home, but thought I could undo the spring. Usually not a funny task. But - both spring bolts came out nice and I could undo the 4 nuts on top of differential. Everything is ready for next week (where I better remember lowering block!!)

All in all a very good evening in the garage. Spring is coming - depression is taking off. Life is good (knock on wood)

Friday, 20 February 2009

I HATE MY LIFE!




But one hour later it was OK :-)





Tuesday, 17 February 2009

Modern rubbish

Here is a picture of the culpruit that stoppet my last season with a annoying gearbox breakdown.

A small circlip that holds the gear in place. Slipped from its place on the mainshaft allowing the gear to slide on the shaft which results in popping out of gear.

This is what happens when inferior circlips are used. Made in china from the standard iron-butter. So soft that the egdes break give in and the clip break away

Crap.












Tuesday, 3 February 2009

GT6 rearseat

OK - to make it up to the GT6 after years of neglect a rearseat was bought. Just really really hope the seller will find the brackets.......


Wednesday, 28 January 2009

OK - gearbox fixed

It's been a while. Gearbox turned out to have the stupid circlip going AWOL. A new - but NOS - circlip was kindly donated by Dave Sideways and installed in box. I am going to install box either this weekend or next (to bloody lazy ATM)

Other news include a megajolt ignition which is currently residing in the basement. Will hopefully be functional on car within a few months (lazy again....)

Thursday, 14 August 2008

Looooong test drive&troubleshooting

Did first leg of RoundDenmark yesterday. Couldn't do second and third leg as I had to work.

Gearbox gave up 50 miles before home - left me with only third and fourth gear. Bit of a pain when you are stuck in stop%go trafick on most busy rpoad in copenhagen area during rush hour. At least now I know the smell of burned clutch (yuck)

Will have to examine the gearbox VERY closely now - I had hoped I could wait till end of season - but unless this is a small problem then yesterday was end of season to me (sigh)

Pictures and more ramblings will follow soon.

Cheers

Friday, 8 August 2008

Gearbox trouble

OK - just when I thought things were good. Only minor troubles, then gearbox starts acting funny. It keeps jumping out of third gear. Not good. I (naively) suspects the gear selector forks - either worn or bent. Will try to fit another top with good forks. If that does not do it - I will have to dismantle the fbox for a rebuild. Till then I just have to do without 3. gear :-(

Tuesday, 29 July 2008

Passed MOT

Whopeee

Passed MOT. Now next mission is to do some serious cruísing (well - that will be when I correct the minor flaws the MOT-man found)

Thing to do:
  • Fit correct headlights - the ones I have is for RHD vehicles - need to be european spec.
  • Do something about wiring of lights - I cannot turn the parking lights on
  • Fix the oil leak from valve cover
  • Find some nuts for the prop bolts that are less fat. Bolts does not engage nyloc properly.
  • Fix slight leak from exhaust manifold - got an annoying whistle

Apart from that - enjoy the summer :-)

Friday, 23 May 2008

Spending time

OK, it has been a while since last blog entry. I have been extremely busy doing all kind of non triumph related stuff, and whenever I started working on the spit I just seemed to get deeper into spit-troubles. Trouble really started brewing when I bought a set of swing spring half-shafts. This was a good deal, and I got a fine pair of shafts. When I realised that these shafts had larger flanges, and would not mate up with the diff - well that were the first set-back. But it was not all bad, as I had a spare diff (a rebuild 4.11) with larger flanges. I just had to swap the two diff. That was setback two as swapping diffs is a bastard of a job!!

Well finally I got diff in and shafts on. Now I could very clearly see that the handbrake cable was to short due to the swing spring shafts being slightly longer. New cable ordered, arrived by mail a few day later. I will not tire you with how I managed to screw the cable up so it could not be used (doh!)

I have also been fighting the dual exhaust trying to fabricate some brackets. Well, lets just say I have been working through a few designs - and even though exhaust is now in place I am not entirely happy.

OK - fast forward a few weeks - had had no time for the spit, but arranged a club meeting, where we would try to start the engine. Engine had been rebuild, but had not yet been started. Everything ran more or less according to plan, and it was very revarding to hear the engine run. However - a bit of water was leaking from the water temp sender in the water pump housing. When I tightened the sensor I overtigthened and ruined the thread on the housing. (another doh!) Well - it was not entirely my mistake as the house was pretty much rusted to pieces. I should have done a better quality check before fiting it.

Well - yesterday evening I removed the rad so I could put a new (old really) waterpump housing on. Got it on, got everything put back together, and started the engine again. Succes.

Engine is running rather rough, but I blame it on the carbs which has not been tuned at all.

Has no pics, but a few from when we held the meeting



Friday, 1 February 2008

Speaking of NOS stanpart

The mad welder took another step towards completeing right hand rear wing. Something had fallen hard on the wreck ruining entire rear wing. Got hold of a NOS stanpart gutter (thing between bootlid and rearwing. Nice to work with´NOS parts. The rear wing is a heritage - not as nice as NOS, but close enough.







More on The Mad Welder and his wreck right here:

http://thetriumphanimal.blogspot.com/

Odd spring and driveshafts

Just removed the old spring yesterday as a part of the conversion to swing spring.

The old spring has caused a lot of trouble - that is positive camber trouble. Looking at the two springs next to eachother explains quite a bit.

Driveshaft will also be changed to the longer 1500 shafts. Should improve handling ( basicly - with that spring anything would improve handling ) If anybody knows what kind of sping i have, then please let me know)

Old and new spring together. New spring seeems longer and lower. Old spring axcactly same height as a GT6 roto spring, but considerable softer.





Thursday, 17 January 2008

More locks, and even more problems!

Well, it took a good two hours to get the passengerside lock to work. I had to grind the lock fork through a hole in the door as I couldn't get the lock (not the door lock, but the part with the key) out. But eventually it worked. Before I fitted the other side, I shortened the fork - saved me two hours work there! But of course nothing is ease. It appears that there has been added a liberal amount of filler around the hole in the doorplate where the lock shall be. And this means that the "legs" that hold the lock cannot engage. This meant another hour of swearing and scraping knuckles before I got all done

During this process I had to remove the locking mechanism - which were to say the least looking a bit tatty. Took the chance and gave it a good clean and a layer of paint. It was very red from a previous respray (by PO). Car is green now, and it really looked YUK.

Before
After


Next week the drive shaft, spring and diff will be removed and replaced by a new parts. Hopefully! I have new AVOs ready, and somewhere in the post is a pair of new longer drive shafts. Some years ago I bought a recon diff from Jon Wolfe. It is a 4.11 but rebuild into a later diff housing (only 4 holes for studs) and with fatter input and output shafts.

Thursday, 10 January 2008

New locks - and new problems!

Finally got around to fit the new WB-locks I bought for the spit. Quite nice locks actually, with nice WB-key set and FS-keynumbers. All good. And much better than other locks in the market, as I do not have to make the hole in the doorplate larger. After a bit of fiddling around, the lock went in very nicely. All very good - until........ I tried to lock the door!


The fork which is engaging the locking mechanism is to long and cannot turn as it touches the reinforcement plate on the doorshell. In the picture below you van see the culprit - it is supposed to turn counter clockwise. Crap! And there is absolutely no easy way to get these locks of the door again.



I will have to remove the locking mechanism on the door to be able to turn the lockforks downwards and gently remove some metal from the fork. Not what I really needed. Thought the lockjob was going to be easy - then again - what is easy with these cars and repro spares!!!

Thursday, 6 December 2007

New boing and bling parts

Got my new AVOs with courier the other day. Will be fitting these pretty soon. Also got a new rear swing spring setup - will probably alltogether transform handling quite a lot.

Just have to get hold of a new spring compressor, got a feeling that the old homemade wooden thing might be fine for 150 lbs standard spring but to weak for 480 lbs



Apart from admirering new shocks, I got around to fit front wing finishers and grille. Nice piece of 70's style black plastick. Looks like I might even make it for a ride in the spring. Can't wait!


Tuesday, 4 December 2007

RBRR2008 TEAM #3

YES, we have secured a good entry number. I have heard that 3 is a lucky number. 3 Danes going as team #3. That must be good.
Now we (well, mostly Daniel as Morten and I are buried in our spitfires) just have to fix the 2000 MK2 (aka The Ferry). Nothing is going to stop us now - well, apart from British technology!

Thursday, 8 November 2007

Fuelpipes

Finally, the last fuelpipes has been routed. Was not quite straightforward, as the carb is a HS4 and fuelpump is for HS2, which means the nozle on the pump points in the wrong direction (MK3 usually routes from pump to carb in front of engine - later routes behind the engine) Not a biggie thou, got the pipe nicely along the firewall.




Basically I am ready to start the engine now. Exiting to see if the ignition works at all - bought at an autojumble. I am just waiting for my engiman Bjarne to come along. I have promised not to start the enginbe without him - healso has some special homebrewed run-in oil with a hint of Molybdenum in it which he swears to.

Wednesday, 17 October 2007

Carbs, ignition and waterpipes ready

Had another go at the engine yesterday. Got the carbs in their proper place - just need to hook them up to the throttlepedal. Ignition also put on, though I am a bit unsecure about it. I was bought secondhand - the old distributor was dead, and this was a great bargain. The distributor is excellent with no play - I am a bit more suspicious about the electronic ignitionmodule. Well - I will give it a try. Of it does not work I will go back to contacts.

I got the waterpipe behind the manifold fixed too.

And to Vitessesteve - thanks for the advice on the waterpumpthread - will try that next week before going up in boltsize.

Finally - managed to push the chrometrim down in the windshield rubber. Generous amount of fairy liquid needed!


Some pics.





Sunday, 14 October 2007

Water pump problems

I - painfully - learned a few things today. First: put the adaptornut (the one for the water return pipe) back into the waterpump housing before you stick it on the engine and puts the radiator in front. Adaptornut cannot be moved one flat with house in situ. That sucks!

Second: check the treads on the waterpump housing before you put everything back together (again). When tightening the alloy thermostat housing the bolt kind of did not bite. and of course there is not any room for a nut under the housing. Going up in boltsize very shortly I believe.

Friday, 5 October 2007

I SEE - COMMENTS!!

Sorry - wasn't aware anybody actually was reading my ramblings and leaving comments. Keep em coming.

Here comes answers:

Thorvald - sorry - I fixed the broken pics now.

Richard - yes - sidewindows and quarterlights are a pain on the roundtails. I beleive I possibly have aquired the last set of sidewindows in the world with the rounded corner. Judging from the price I would say they are very rare. Hope deal goes through. Othervise I must resort to the modify softtop thing.

Vitessesteve: Yes - nice patches - may hold water for a while, but certainly not pretty, and a sure place for rust to start eating again. Been replaced (and a the same time I could straighten out the damages from the sideimpact by a previous owner - he must have forgot to tell me somehow - ehh???)

Thursday, 4 October 2007

Yours truly doing Round Denmark - 2000 kilometers, 36 hours













Tuesday, 18 September 2007

Engine is back in!

Finally - and after much struggle - the engine is in right back where it belongs. It was amazingly easy to get the engine in. Now things start to come together, and I hope that the car will hit the road this spring. Has started to fit all the life support systems, work of joy really. After being stuck for 4 months I can finally report some decent progress.
Here is the pics.






Wednesday, 11 July 2007

Sæder til salg!








Send en mail på nikolaj.blomberg@gmail.com hvis du er interesseret. Sæderne er i rimelig stand. Vinylen er pæn, men der er et par små huller i stoffet. Skummet har set bedre dage, men er udskifteligt. Sæderne har sunde rammer og gode sædeskinner.

Det er 1500 reclinersæder inklusiv nakkestøtter.

Friday, 1 June 2007

Engine and gearbox ready

Yihaa, installed the clutch, bolted up the gearbox. Now it is just about ready to go in!

Thursday, 31 May 2007

Seeing things in the right perspective

Now, things have been a bit slowgoing lately. To be honest, things have been boring. I am getting nearer the end of restoration, and have reached the dreaded last 5 %. Anyway, I get a little happier when I watch the rather artistic patchwork some PO did in the footwells. Clearly illustrated in the pictures below

Sunday, 20 May 2007

Outrageously slow updates!

Sorry for the lack of updates, things has been pretty frantic lately. Anyway, good news; engine has arrived.

Engine has been proffesionally rebuild, and was delivered last friday. I took a day off and painted the engine matt black (actually same colour as the window frame)

I also fitted the clutch. Had intended to put the gearbox on, but realised that I had forgot the seal at home (the seal that goes between the bellhousing and the gearbox)

Hopefully I will be able to put gearbox and engine back together next wednesday, and throw the entire unit in the car. This partly depends on testing the solenoid on the OD - haven't had time to do this yet. If it turns out OK I am ready to proceed.

No pictures in this update as I am presently operating on a 56K telephone modem. sigh!

Friday, 9 March 2007

FLASHING!

Another few hours, and the front flashers and one headlamp could be taken of the to-do list. Nice.


Monday, 5 March 2007

Slow, but steady!

Oh dear. Only one night i the garage, and only one update to the blog i February. I certainly got to speed up if I want to don the Round Denmark Reliability Run in this car!

Did pop by the other evening, though I didn't manage to do much. Got the bonnet locks on. They aren't pretty, but they work!

Also cleaned an old front trunnion that was broke due to neglecting lubrication. I had the doubtful joy of driving the spit with this trunnion just two weeks before it failed. I was driving rather spirited in the countryside. Scary when I think about it. It lost its front wheel 2 weeks later. To judge by the rust in the broken link I believe that it was already broken when I drove the car.

Morale: Don't forget to oil your trunnions regularly

Friday, 9 February 2007

More progress (well - a kind of)

I must admit - it is very cold outside at the moment. Unfortunately - when it is cold outside, it is also cold in my garage. In fact is is so cold that the batteries in my camera went dead. (perhaps just a bad excuse for not charging them?)

Anyway, I did actually manage to do a few things before I froze to death (nearly) I attached the little handbrakecable spring that always go missing on these cars. I would not miss it now if it got lost - it was awful to get in place!

Second I fitted the rearwiev mirror. The very clever man who had treated the windscreen frame with new vinyl had forgotten to mark where the holes for the mirror were. After what felt like a really long time I found the hole and could punch through the vinyl.

Front valance also went into place. Nice little job - wish I had smaller fingers!

Replaced the door handle I put on last week with one from the shelf that was in a better condition (whoa - if I keep up this I can do everything twice - I need to get my stuff sorted out!)

Finally - I put on the bonnet stay. A bit tricky since I had none of the proper bolts. Previous owner used whatever he could find.

Over and out - going away for a looooong week.

Wednesday, 31 January 2007

It's all clear now - finally!

Finally some decent progress. Yesterday I had some good quality time with the Spit. Managed to fit the front windscreen - this time without breaking it. It was actually rather easy to get the glass in once I had read the manual. And this time I read it a bit more thoroughly than last time!

I didn't manage to get any pics while working, but here is a picture of the window in place!




As one can see, the second thing I got around to was fitting the bonnet. I have had this job waiting since god know when. But didn't want to do it before I had the engine in. Well now, since I have been waiting more than a year for the engine, I can just as well put the bonnet on now and get the door gaps adjusted. That's a job for next time.


When door gaps and windscreen is adjusted I can fit the glove boxes. Hope I hit the road by spring!



Front end is sitting quite high due to the lack of an engine.


A spot of masking tape can be seen running along the lover edge of the front wing. I am bitterly regretting that I didn't remove this last summer, as it is a pain to get of now. I spent quite a while last night removing it. Just another hour or so left! Hooray

Friday, 26 January 2007

I am stuck - and it sucks!

Yet another Thursday in the garage. It was bloody cold though, and I didn't get anything done (apart from putting on a door handle - pathetic really!)

Problem is that I am stuck. I would like to put on the door cards, so I can say doors are done now. But that's a no go since my windows is still in England - and I am waiting to get them shipped to me (get the drift James?)

Okay, I could put the panel covering the gas tank on - nooooo - have to wait for the bolts goes into the diff - rear end are lowered, and for some reason I have been supplied with wrong bolts.... Crap.

Okay, how about the exhaust - that really need some work. Nope - can't do without engine (still out of town, has some problems with the oil temp sensor which is going into the sump.
No engine - no gearbox.

Okay, what about the glovecompartments then. Nope - forgot the cord which I need in order to fit the windscreen. If the window frame isn't properly adjusted - it's a waste of time fitting glove compartments.

How about adjusting the doors the - no can't do without bonnet in place, can't put bonnet on without engine in.

On top of this it was something like 10 degrees below zero - cold cold cold cold!!!!

Should I go on??? This sucks!! I want the car ready for spring.


Notice the fancy red paint on the door striker - just visible in the door gap. Looks awful - should have given the striker a good cleaning before I fitted it. Alternatively the moron who painted the car red years ago could have used masking tape. (moron! (me that could just as well be - moron, not painter that is!))


So after 5 hours I could evaluate the evening - I managed the impressive job of fitting a door handle (max 10 minutes!). At least I took a picture. Hope next Thursday will be better.
At least I got around to sweep the floors!
Next Thursday front window goes in ( and hopefully I will not break it this time!)

Thursday, 18 January 2007

Work work work

Dropped by for a few hours Tuesday night. Forgot the camera though. Spent most of the time scraping old rust treatment of The Wreck (Mortens new acquisition - follow link top left). Dirty boring work really. Though at the time I found it more appealing than working on my own spit. The last 5 percent is so bloody boring. I did eventually - very late - fit a Lucas sports coil and tightened the water hose clamps from the heater to the heater valve. They were finger tight only. So I did kind of work a little on my own spit too. Can't wait to finish it and start the GT6 project!

Friday, 12 January 2007

We're back - and working the Spit

Finally I got time to go to the garage. Had a minor fight with the doors trying to get all the stuff inside them lined up. Pretty simple - if you pick the right bits of the shelfes first time!

Got around to fitting the last of the extra instrument - an oil temp-meter. Now all three is nice tugged away in the bracket. From left: amps, oilpressure, oiltemp. The bracket is a Lucas bracket I have picked up sometime in the past. Came with a nice little bag with bolts and nuts. I had to modify the bracket slightly to get it in line with the other instruments.





My engine man called me today - the engine is close to finished now. Had had a little trouble trying to get the oiltemp sensor fitted to the sump. Hope to have my engine running within a month.