First - sorry - no pics.  When I wanted to get a few pictures I realized (again) that the battery on the camera was flat.  That's second time recently this has happened. Better get some fresh batteries soon.
Still - I have had some fair progress.  The exhaust prop and engine are all bolted back together fine. I took the inlet manifold of and drilled 4 holes in it for 
vacuum. First a 2mm pilot hole. Then a 4,2 mm hole and 
finally tapping for 5mm thread.  Went quite smooth was OK result. I have had some problems with the choke sticking. It is a 
SU1.5.  It has been converted from 
waxstat jets to proper jets. Problem is (I think) that the links used to convert isn't all perfect and creates a bit of tension. Morten and I tried messing with the links to see if we could release a bit of he tension. After quite a bit of fiddling the choke got better - not perfect - but better.  
Carbs went back on - all nuts on the manifold studs were tightened.
I found out I had forgot to put the radiator overflow bottle back on when I put the radiator in. Bit of a problem as the radiator has to be tilted a bit to get to the bolt where the 
overflowbottle-bracket attaches. So - undo 6 radiator bolts - 
overfowbracket in. Tighten bolts again. Mission 
accomplished.
Finally I put in a very neat bit of wire harness that The Mad Welder had made for me. I am 
converting from dynamo to generator plus a few other thing. So I needed a new harness  for the generator, the 
oilpan temperature and 
halogenlights. But it was made perfect and very easy to fit.  Thanks Morten
Enough for this time.  Next time I get to spend a bit of time with the car I will try and start it.